MY FIREBREATHING 2JZ 240SX Hits the Dyno! BLUEJZ MAKES POWER!

The Blue Jays II: A Year and a Half in the Making

It was a cold Georgia day when the moment finally arrived, after a year and a half of struggles, for the Blue Jays II to come back to life. The team had faced numerous problems, but with the help of Pineapple Tuning and Mr. James, they were able to overcome the obstacles and make the car sound "absolutely huge." Mr. James was an amazing source of inspiration, as seen on his YouTube channel, which provided invaluable assistance in preparing the car for its return to life.

As the team began their journey, they made sure that everything was in order, including checking for any loose wires or connections. They also took the time to ensure that the boost controller was set to the correct pressure, which revealed a surprising finding: there was only 10 pounds of spring in the car. This was an important discovery, as it allowed the team to adjust the boost pressure and make further modifications.

One of the most significant challenges faced by the Blue Jays II was the issue with the fuel pump, which had been failing on them for some time. The coil packs were also deteriorating, but fortunately, they were ancient enough that this was not a major concern. However, the team decided to conduct an experiment to determine if the fuel pump was indeed the culprit behind the car's recent problems.

To do so, they created a poll and asked viewers to share their thoughts on how much boost pressure would be needed to solve the issue. The results were astonishing, with 412 horsepower being achieved when running the wastegate alone. This was an incredible feat, and the team was eager to see what would happen as the night went on.

As the temperature continued to drop, the team made adjustments to the boost controller, adding 1/8 of a turn to increase the pressure. The results were nothing short of remarkable, with the car producing 494 horsepower and exceeding the desired 500-horsepower mark. This was an incredible achievement, considering that only 400 foot-pounds of torque had been achieved just moments before.

The team was thrilled with the progress they had made, and it was clear that their hard work and dedication had paid off. The Blue Jays II was now sounding better than ever, and the team couldn't wait to take it for a spin and experience its full potential. As the sun began to set, the team reflected on the day's events, grateful for the support of their audience and looking forward to their next adventure.

The power of the Garrett 3071 R turbocharger was truly awe-inspiring, with its incredible sound and ability to deliver such impressive results. The team was thrilled to be working with this engine, and they knew that it would play a crucial role in helping them reach their goals. As they closed out the day's filming, the team couldn't help but feel a sense of excitement and anticipation for what the future held.

Finally, as the day drew to a close, the Blue Jays II had achieved its goal of reaching 500 horsepower. The team was overjoyed, knowing that all their hard work and dedication had paid off. They took a moment to appreciate the car's performance, marveling at its smooth and healthy power curve. It was clear that this engine was special, and the team was grateful to have it as part of their project.

The experience had been a long and challenging one, but in the end, it had been worth it. The Blue Jays II was now back to life, sounding better than ever and ready for its next adventure. As the team packed up their gear and said their goodbyes, they couldn't wait to see what the future held for this incredible car.

"WEBVTTKind: captionsLanguage: enokay so today is the day at this very cold Georgia day Blue Jays II finally lives once again a year and a half later so many problems so when he struggles to get over lots of long nights absolutely huge help from pineapple tuning and also mr. James would make sure to check out James Woods YouTube channel because he was an amazing help TV before oh my god I was not ready James how do you feel about today well they fall off yeah crank along just to feel that make sure nothing's rubbing or anything so halfway through the RPM civic SI all motor built 218 315 torque yeah okay it's been a long time coming but we're finally at the dyno finally got blue JC on the rollers sounds amazing I forgot how awesome this thing sounds we had the powerhouse racing bottom in so it's built to last I'm super excited but let's see what it does first we got to do like the cruising tune and then drive it around going in and out of our hands make sure everything's buttoned up because that is something a lot of people overlook they only focus on both are on the holes within the rest they're tuned absolutely sucks so we'll see how it goes so one thing we actually didn't know is we can't remember what's spring we had your wastegate so hey the best way to find that out is if we turn your boost controller all the way down which means there's no boost leak now we're just straight running on spring pressure it comes out to 10 pounds so you have a 10-pound spring in the car which is good to know and we can basically go up from there and figure out where it needs to be but just how many loose clothes work is it's a controlled loosely so you can either bleed more boost off or take it out and that will determine what level you're gonna base behavior okay it's now night time now it was a very long time is the last foot because we went on a little adventure because the fuel pump was dying on us therefore it was breaking up and the coil packs were pretty much dying too but they were ancient coil pack so it's okay so now we're gonna do one more test to see if that was the full problem causing that little breakup you saw earlier so we just made a poll and on in the pounds of boost basically just wastegate they made 412 horsepower that is ridiculous okay so we've done half a turn on the main dole boost controller let's see what happens as the night goes on we're making more power but unfortunately gets colder and colder and colder sight just keep bundling up but I'm looking forward to seeing the final results honestly I'll be really happy if we just match what we had last time which was right around 510 wheel horsepower because the car was so much fun to drive at that power level it felt balanced but almost to the edge right with you had any more power and you went up with the mountains up it'd be a little crazy so that's what I love about this car is going into the mountains taking back roads that's my favorite thing to do in this car so 500 is like more than enough and if we ever want to go more power we can always you know upgrade the fuel pump if we could also put a bigger turbo on it but this Garrett 3071 R is absolutely incredible that is the best sound ever all right eleven point five pounds of booze for 39 for a tutorial 4:53 gettin closer okay just hit 470 Megan progress and how many pounds with that Mikey thirteen pounds still on this little bitty GTX turbo it makes it so hard it it's already described because in person it's so much more crazy than it is on camera but it's pretty amazing film sounds so good for them next turn okay okay so 482 we're making progress I'm actually excited now okay you're making good progress I think we've got one more pull in us and we're kind of running out of fields still I have 850 injectors but we don't want to completely have 90% plus duty cycles to keep it manageable to keep it safe and at the same time as you see James behind me is using the turbo to warm himself up no clothes we turn up the boost controller by 1/8 like just in and it went all the way up to a 494 it's rigged so awesome man finally we don't hit 500 I wouldn't be like bummer but nothing like substantial we're doing four hundred foot-pounds of torque as well so I was like four to twelve about the tort before our last poll I know my god I told me that so much it made for ninety-nine point 50 why John that's not fair that is not fair at all however the curve is insanely healthy so that's the more important thing BAM that's what Siri if you look at the graph smooth it is that's what zero smoothing so this is 5:13 at the very end at the end of the day blue jay-z made 500 again and it is awesome cannot wait to drive it I'm gonna close it out because it's like two of the more days but other than that thank you guys so much for watching this video I upload every Tuesday Thursday and Saturday and have a wonderful day thanks for all the support see you next time you\n"